1995 KDX 200
I purchased this bike a couple months ago as a winter project and started in on it. Rode it a little but ran pretty crappy. It did make pretty good power though, but could immediately tell a few things were off, so I dove in.... when I got it, it was what pretty clear it had not maintained at all, but I paid next to nothing for it so.......

Just sent out the head and carb to RB - looking forward to getting those back! Anyway, I was going to go ahead and pull the jug while I had the head off and do the KIPS valve cleaning and inspection and inspect the piston. Looks like this had been done in the past at some point, and the piston looks too good to be the original. Top of the piston looked great with a good burn profile. Didn't see any scoring in the cylinder from the top or front exhaust port. When I took the right side cover off to pull the KIPS shaft apart and remove the jug the PO had completely rounded off the nut for the shaft.

